Updated the Pusher foot on my LNL-AP Brass feeder

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Blue68f100

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I had used a leather pad stuck to the bottom of the factory feet for nearly a decade. The pad would come loose requiring me to glue it back on.

Since I now have a mill I decided to make something more permeate. Factory design vs my new one.
New vs Old pusher foot.jpeg

I machined this for it to work with a case as small as 380/223 up to my 45 acp. May work with a larger caliber but this is the largest I normally load on it.
New foot w-45acp.jpeg
New foot w-45acp.jpeg

This show the flat section that now contacts the brass fully at the base so the brass does not tilt.

New foot sized for 380 up.jpeg
And one last photo showing the brass feed pickup. This is a smaller inside diameter down tube than supplied. With the smaller ID the brass lands straight and does tilt.
New Brass shute.jpeg

I loaded 600 rounds of 45acp last Saturday and did not have a single hick-up, brass feed or otherwise. During my testing I found if you had a kink in the brass retainer spring, it caused the brass to raise up, causing a bind into the shell plate. So as long as a kink does not get in the works it runs 100%.
 

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I agree with Walkalong, Very nicely done.
I finally took Walkalong's and other's advise and ground my subplate back to ramp the spring down at station 5 and have not had a kinked spring since.

That looks like it was a royal pain to machine out. But I bet you'll find out it was worth every minute you put into it. Good Job.
 
My base has been ground back for almost as long as I have had the press. My current case retainer spring is like 4 yrs old and only has 1 kink in it. So I've been doing pretty good. I only get into a problem if the kink ends up at the edge of the case, other wise it just rides over it.

As far as machining, I had a 90 deg V cutter and angle blocks to adj the tilt. Spent more time setting up than machining.
 
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