mc223
Member
Over the past few months there have been a few threads about bridging and related problems with Varget and other stick powders in Dillon powder measures and small mouth cases.
I had the same problem with mine, so I set out to cure the problem. First came polishing the drop tube. Helped some, but still had an occasional mess to clean up. So I used a taper reamer to enlarge and smooth the drop tube followed by an extra fine polishing. Much better but still got a bridge about 1 in 250 rounds.
I worked at a place once that mixed chemicals. Mostly granular type stuff. They used shakers to keep the stuff flowing.
I used a small sealed electric motor and a piece of 1/2 in scrap steel mounted to the motor shaft like the one used on tumblers. This assembly was then mounted to the Dillon Strong mount and wired to a dimmer switch to control the shaking force.
Powders flow smoothly and more accuratly. And since the whole machine is vibrating there is some settling of the powder in the case, which reduces the old familiar crunch. Bullet seating seems smoother also.
I had the same problem with mine, so I set out to cure the problem. First came polishing the drop tube. Helped some, but still had an occasional mess to clean up. So I used a taper reamer to enlarge and smooth the drop tube followed by an extra fine polishing. Much better but still got a bridge about 1 in 250 rounds.
I worked at a place once that mixed chemicals. Mostly granular type stuff. They used shakers to keep the stuff flowing.
I used a small sealed electric motor and a piece of 1/2 in scrap steel mounted to the motor shaft like the one used on tumblers. This assembly was then mounted to the Dillon Strong mount and wired to a dimmer switch to control the shaking force.
Powders flow smoothly and more accuratly. And since the whole machine is vibrating there is some settling of the powder in the case, which reduces the old familiar crunch. Bullet seating seems smoother also.